headspce was consistent to within .001
case head was spot on everytime .372
widest part of the body was spot on everytime at .379 (not on new brass though as my chamber is quite losse so once fired brass fills it out but it was the same between the brass that chambered and the brass that wouldnt chamber)
case neck .226-.227 (spot on)
the brass definately doesnt need trimmed as at its longest it 0.030 off the full length of the chamber.
the only thing I can visually see is at the base of the case neck on the one of the rounds that wouldnt chamber is it flows out toward the shoulder instead of straight down. I have only neck sized 1/2 the neck on the first loading of the brass and the second loading, I dont lube as my previous brass never needed it, could the new brass need lubed and therefore when I neck size its sligthly catching pushing the case neck downwards on the up stroke due into the neck sizer die to too much friction catching the brass instead of pushing over it, and making thee brass bulge out therefore not allow the case neck too enter the chamber? Though surely this would happen on my first loading as well as I neck size in the same way or maybe each time I size it gets a bit bigger? They definatley couldnt need full length sized as headspace is consistent with brand new brass as in once fired brass. I am open too all ideas and opinions as I am still quite new to this relaoding game and am a bit stuck on this one.
Its not all bad though I have hit a nice laod, after I had this problem tonite I just blasted off my last few rounds and shot a nice 5 shot .350 group without trying much
